Okay, so anyway, on to the A/C work.
When I got it, the car had all the A/C stuff except for the compressor, dryer, and the low-pressure hose from the dryer to the compressor. I'm not sure where they got to or why they were removed, or for how long they were missing, but I tied down the high-pressure hose, and ran it like that for a few years. Since then I collected a used dryer and evap-dryer pipe and a new dryer-compressor hose. Dale's red car donated the compressor... I think. I'm not sure where mine came from really but I had a couple and this was the best of them. I got a new dryer, a new R12 orifice valve, and a R12-R134 retrofit kit from FCP Groton, and forgot about them for at least a year.
This winter one of my only tasks was to finally get the A/C working. I'd decided pretty early on that I was going to use Dura-Cool for simplicity, and I gave a list of reasons for the decision earlier in the thread. Here are some details of what I've done:
The first step was to clean everything. Brakleen was recommended by Art at Cool Earth, as it's cheap, has great cleaning properties, and is a hydrocarbon so any residue is not going to mess up the system. I had a pretty good sized bottle on hand, so I went to town:
I scrubbed away at all the hoses, the silencer, and cleaned off all the sealing surfaces. I flushed out all the hoses and the silencer with brakleen and then blew them out a couple times.
Then, after removing the orifice and hooking the HP line back up to the evaporator, I filled the evap through the LP return nozzle and blew it out with shop air. This blew the brakleen through the one hardline I couldn't easily remove, through the condenser, and out of the fitting that would drop into the silencer once it was reassembled.
I used about half of it. I was getting some nasty looking fluid in my catch pan:
But I kept going until it came out clean. I then blew it out for 5 minutes straight, hoping to get all the residue. I reassembled the system using the new orifice, dryer, and all new seals except for the one that I couldn't get to without removing the front bumper.
Following Art's instructions, I poured 2 oz of Dura-Cool's Oil Chill lubricant into the dryer, 2 oz into the evaporator, and 3 oz into the HP line coming out of the compressor (which pools in the silencer just before running through the evaporator. His rule of thumb was 2 oz for each of the exchangers, 2 for the dryer, and 1 oz for each 10 feet of hose. Then the compressor went on and 6 oz of Oil Chill was poured into it: 2 or 3 oz into the inlet fitting and the rest into the reservoir. There isn't much magic here apparently - it'll all equalize is what he told me.
All buttoned up:
Oh yeah, and I scrubbed away at the compressor pretty good too. I pulled off the clutch assembly and painted it up while I buffed the compressor body with a progression of scotchbrite roloc discs. No fancy polishing here, just some good mechanical cleaning.
Because of the mix of Eagle and Volvo parts, I was forced to do some fabricating when it came down to the bracketry. The Eagle has a different way of mounting the compressor, since it uses a serpentine belt arrangement, but because I foolishly used the Volvo V-belts, I needed to come up with some form of tensioning device. It was pretty simple - a tensioner from a Ford A/C system and a bodged together slider strut. It's all solid as a rock and lined up properly so I'm pretty confident that it'll go the distance. I failed to take any pictures of this so far.
Anyway, once it was all buttoned up I gave the compressor a bunch of turns by hand to make sure it wasn't hydraulically locked, per Art's instruction, and pressurized the system with shop air to see if it would work. And it did! Clicked on and off nicely, the compressor ran quietly, and all appeared to be working well. I left the system pressured up for a week and it did bleed down a bit, so I went over all the fittings with soapy water and found a slight trail of bubbles coming from the brand new R134 fill fitting I got in the seal kit! A quick twist of the schraeder valve and a bit more air pressure, and 3 days later no difference. Sealed!
I booked the car into Cool Earth's install bay (officially named My Automotive Shop... really!) and got them to pull a vacuum, purge the system, and pressure it up. I could have done this last part, but I'll keep my cans for top-ups, in case of any leaks too slow to detect over a 3 day period. Art pulled a vacuum for 2 full hours before his gauge bottomed out - you pull a vacuum to boil off any moisture in the system, which will freeze and collect in the orifice & render the system dead until it thaws out - and left it there for another couple hours to verify that it was still sealed up. All seemed well, so he purged it with inert gas (you'll want to start charging at around atomspheric, I believe, but you want to keep all oxygen out of the system) and then charged it with Duracool R12A replacement refrigerant. He ran it hard for a while to ensure system operation and no freezing, and he declared it to be in great shape. 38 degree outlet temps and a quiet compressor (and poorly hidden amazement that an '88 Volvo could look so good).
The vacuum/purge/refill cost me $190 after tax, but I'm happy about spending it there. I don't have the equipment to properly vacuum the system (it needs to go to about 28.5-29 inHg, the car's motor only pulls about 14" and the car coupled with a cruise control vacuum pump only pulled about 22") so at least I know it's done right, and have a more experienced eye tell me that the job was done properly.